Re: After a Big Sleep - #4612 Rolls Again !!!
Reply #25 –
Rear axle was geared too low. Designed for 55mph as you surmised. I sent the new coaches to Unitrax the local axle service center and had the rear end regeared before delivery on my customers 91's.
Went from 3.91's to 3.21.
Mileage and hill ability was with the 3:21's. Beaver changed the production coaches after my factory stores good results with the change to the gillig chassis.
Would only go 68 before. Customers did not like that at all.....
Fixed.
Was going to regear my m11 but the engine so far does not seem to have enough torque or horsepower to benefit from regearing the coach compared to many other coaches I have driven over the years.
Went to a less power consuming hydraulic fan drive thermostat and installed a bit noisier 5050xl resonator.
Last step after four years of work so far is to take the coach back to the la cummins facility and dyno it again.
Still possible turbo or injector long term issues. You never know until tested or fixed.