Re: Test drive with new resonator
Reply #39 –
Ok.
5050xl Resonator
Donaldson blue foam air filter
Replace Winn system with a Parker/rancor
Replace fuel lines
Replace bad cam position sensor
Replace updated air pressure sensor
Adjust valves and injectors
Replace tires with fuel efficient Michelin zxa-3+
Rebuild alternator as it had a bad diode.
Add 270 watt solar to basically turn off the alternator driving.
Leave the solar set for 13.6 volts at the battery which matches the alternator output at the battery.
Replace the dynamatic 180 degree max on hydraulic fan control with an industry wide use 199 to lessen unnecessary hp loss.
The way foretravel built mine the fan was on high speed if the motor was at operating temp.
-50 hp versus at idle speed -15 hp?
90/100 psi in tires. Synthetic lube in front wheel bearings.
Partial transynd in trans.
My opinion is that the tires helped the most followed by the fan controller.
Easily noticeable that the coach has less rolling resistance.
Less retarder use where possible.
I have no idea if the mpg results I have seen are helped by my work and/or the engine has less power than others maybe because of issues still undiscovered?
Power is better especially the torque in the upper gears.
Also possible that the engines computer alters the power from cold to warm.
Possible that the overly on fan control caused the computer to hold back some power.
Would have to change the controller back to maybe see.
Or is it just the tires and exhaust?
Or just the fan?
Hard to know.
Works well enough now I am ok.
Need feedback on boost psi on others. Mine used to top out in low altitude small grades at 28 pounds now hits 31 or so revved up in fourth
Expensive resonator job as the dealers guy ordered specific curved sections and welded everything beautifully.
Versus more flex tubing? Unknown.
I would trade the mpg for more power but not really needed just wanted.
Hope this helps. The exhaust really helped free up the motor