Re: 10kw Powertech issue.
Reply #5 –
Just paid a lot to have my local cummins dealer replace a major gasket that leaked oil and the oil pressure sending unit.
Plus glow plugs. And adjust the valves and injectors. Much smoother. Unknown hours but probably high as the hour meter was disconnected and the coach home based in pheonix.
Not your same motor as it has the izuzu three cylinder.
My previous servicing done by myself seemed to me to find that the hoses on the gen were slightly too short. Had to go around the head leaving an air bubble in the system.
Unknown if the hoses on ours were original but when I did it the reinforcing wires inside had corroded away.
So they ordered the hoses both slightly longer and now they fit over the valve cover and allow any air bubbles to be removeable.
But the hoses now are tighter to the compartment light.
Yes I found the pain to remove block drain which had never been touched before to drain the block which I did and I flushed it.
Now had the dealer drain the block. Replace the hoses with longer ones and replace the electrical breakers.
Under heavy gen loads I had the fan and main 45's pop a few times and their spring action felt slightly weak.
New ones feel identical but so far have not popped.
Replaced the water pump drive belt also as its condition was unknown.
Sorry for the long post but the shorter hoses made removing any air bubbles harder on our coach