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Topic: Results of ten coach bucks spent (Read 1214 times) previous topic - next topic - Topic derived from Re: Engine Fan vs two...

Results of ten coach bucks spent

Last May we spent just over $10,000 on exhanst manifold. a new head, turbocharger,and after cooler core. Our fuel mileage has jumped from about 8 to 9.6 driving down from Illinois on I-74 to I-75 then on down to I-10 in Florida. If you've driven any of that you know the hills seem to be never ending. Once in Florida and level roads we got up to 10.6! We are pulling a Malibu and keep the fuel up near the top until the price jumped. the 8 mpg was pulling a PT Cruiser that's a lot lighter. With no leaks in the intake system the whole thing ran smoother. It did hills without shifting. Feeling pretty good about the money spent!  ^.^d 
Larry
1996 U295 36'
Build # 4805
Actually we sold it but just like to lurk

Re: Results of ten coach bucks spent

Reply #1
Last May we spent just exhanst manifold over $10,000 on a new head, turbocharger,and after cooler core.

Turbos go bad with too much boost & heat, that's a given. What engine is that, and what caused the head to have to be replaced? Mileage when the work was done?
1993 U-240 "La Villa Grande"..CAT 3116 w/ Pacbrake PRXB...Allison 3060 6-speed..
Previous: 1983 Airstream 310 turbo diesel, 1979 Airstream 280 turbo diesel
                                      Build # 4297
                                      PNW natives
                      Home base:  'Cactus Hug' (Ajo, Arizona)
                        DW Judy & Chet the wonder dog
                        Full-Timers 'Sailing the asphalt sea'

Re: Results of ten coach bucks spent

Reply #2
Engine will be the Cummins C 8.3 liter.
Brett Wolfe
EX: 1993 U240
Moderator, ForeForum 2001-
Moderator Diesel RV Club 2002-
Moderator, FMCA Forum 2009-2020
Chairman FMCA Technical Advisory Committee 2011-2020

Re: Results of ten coach bucks spent

Reply #3
Always fun when an improvement/repair works better.

Only way out of the coach bucks is to drive the $'s out of the coach in use...
"Riding and rejoicing"
Bob
1997 U320 40' Mid entry, build 5132,  wtbi ce27, 4th owner
2007 Solara convertible
2 prodeco tech outlaw ss electric bikes

1095 watts solar
08 Ls 460 and a sc430
2000 Ford F-250 superduty 4x4

Re: Results of ten coach bucks spent

Reply #4
Always fun when an improvement/repair works better.

Maybe for you high rollers, but 10CBs for an "improvement/repair" seems a bit much. Perchance, this was a high mileage coach, with not much service, and the driver had "his foot in it" often?  :-\
1993 U-240 "La Villa Grande"..CAT 3116 w/ Pacbrake PRXB...Allison 3060 6-speed..
Previous: 1983 Airstream 310 turbo diesel, 1979 Airstream 280 turbo diesel
                                      Build # 4297
                                      PNW natives
                      Home base:  'Cactus Hug' (Ajo, Arizona)
                        DW Judy & Chet the wonder dog
                        Full-Timers 'Sailing the asphalt sea'

Re: Results of ten coach bucks spent

Reply #5
Head itself was OK except for the many bolts broken trying to take the manifolds off. Decided that since Cummings had the mounting holes in little ears rather than into solid block material the cost of trying to get that many out without breaking the ears off was too high. Compare new valves and seats, injectors, etc with paying for someone to try to take the broken stuff out with no guarantee of any success. The exhaust manifold had shrunk to where the ports wouldn't line up with the new head. Kinda a when it rains it pours. Took it in originally for oil and filters and valve adjustment. Coach has 167,000 on it.
Larry
1996 U295 36'
Build # 4805
Actually we sold it but just like to lurk

Re: Results of ten coach bucks spent

Reply #6
Wow that's s chunk of change! Isn't it strange how "these engines last thousands of miles in big trucks" kind of like my 6 coach bucks for an CAPS injector pump at 80 K miles.
Bruce, Linda, and Macy
Zoey RIP 1/20/19
1999 U295 40' build #5400
2017 silver Jeep Wrangler, 1260 watts of solar on top
Moving around the country

Re: Results of ten coach bucks spent

Reply #7
 "Bubba's R.V. Repair" has this illusion we are  all packed with the coin of the realm. The only honest one was a shop we stopped at, since I knew I had a noisy valve. The head tech said, "these coaches freak my guys out, they're afraid that they're going to screw other things up." I found another shop in Flagstaff where the guy said, "we don't care, an engine is an engine". They put down carpets, wore plastic over their shoes, and got the valve train adjusted!  ^.^d
1993 U-240 "La Villa Grande"..CAT 3116 w/ Pacbrake PRXB...Allison 3060 6-speed..
Previous: 1983 Airstream 310 turbo diesel, 1979 Airstream 280 turbo diesel
                                      Build # 4297
                                      PNW natives
                      Home base:  'Cactus Hug' (Ajo, Arizona)
                        DW Judy & Chet the wonder dog
                        Full-Timers 'Sailing the asphalt sea'

Re: Results of ten coach bucks spent

Reply #8
Head itself was OK except for the many bolts broken trying to take the manifolds off. Decided that since Cummings had the mounting holes in little ears rather than into solid block material the cost of trying to get that many out without breaking the ears off was too high. Compare new valves and seats, injectors, etc with paying for someone to try to take the broken stuff out with no guarantee of any success. The exhaust manifold had shrunk to where the ports wouldn't line up with the new head. Kinda a when it rains it pours. Took it in originally for oil and filters and valve adjustment. Coach has 167,000 on it.

Larry...the new head has the same "ears" or did Cummins improve the design....?

Hans
Hans & Marjet
1995 U300 "Ben" (#4719)
3176B Cat,4060HD,Jake
SKP#139131
Motorcade#17579
2006 Honda Element (towed)

Re: Results of ten coach bucks spent

Reply #9
Be thankful that you are getting more power and better economy. I got hot water for my 9.6 CB's.

Mike L I agree with you but would add that all MH shops assume every owners name is "Warbucks"  :))
Jerry & Nona and Kimeru the cat that thinks she's a dog
1998 36' WTFE U320  #5314 Motorcade #17711
USAF 1975-1995
2019 Subaru Crosstrek 'toad'
2003 Subaru Legacy touring car
jerry Fincher | Flickr

Re: Results of ten coach bucks spent

Reply #10
Larry,

Any idea why all that stuff needed repair.  I can tell that my exhaust manifold has shrunk, but there are no leaks or broken bolts, so I am not about to touch it.  I have thought about pressure testing the after cooler to see if it has a leak.
Jerry Whiteaker former owner 96 U270  36' #4831 Austin,TX-Owner Mods LCD TV w/front cabinet rebuild - LCD TV bedroom - Dual Central AC, either can cool coach w 30 amp - Skylights at roof AC openings - Drop ceiling for ducting of AC - Shower skylight white gelcoat/wood/epoxy frame - Air Springs/Shocks replaced - 2014 CRV - 8K Home Solar - Chevy Volt

Re: Results of ten coach bucks spent

Reply #11
8.3's ,while reliable, are not in big rigs.  A m11 is at the lower end of heavy duty Diesel engines on a chart and were used in some big rigs. 

As far as I know
"Riding and rejoicing"
Bob
1997 U320 40' Mid entry, build 5132,  wtbi ce27, 4th owner
2007 Solara convertible
2 prodeco tech outlaw ss electric bikes

1095 watts solar
08 Ls 460 and a sc430
2000 Ford F-250 superduty 4x4

Re: Results of ten coach bucks spent

Reply #12
"Take me down to Coach Buck City, where the money's green and the coaches are purty."

Re: Results of ten coach bucks spent

Reply #13
"Take me down to Coach Buck City, where the money's green and the coaches are purty."

This guy is good, if I would of had a swig of beer in my mouth it would have exited my nose! Now I just have to stop the music from playing in the background of my mind. Please take me home.

Rock on
Old Phart Phred, EIEIO
89 GV ored 36' #3405 300 hp cat 3208 ATAAC side radiator, mountain tamer exhaust brake

Re: Results of ten coach bucks spent

Reply #14
I'll have to look tomorrow to see if this one has ears. Two of the broken bolts were laying on the block. Don't know how long they'd been broken. The exhaust manifold would have been OK if it didn't need to be taken off. Of course, then it wouldn't fit back on the new head. I had often wondered about the after cooler having leaks due to the persuasive display at my service dealer. Just never got around to it. The only think that went from one thing to another was the broken bolts leading to the head. A tech noticed a small hole rubbed in the after cooler and it was soldered then tested. Did I mention about raining and pouring?
Larry
1996 U295 36'
Build # 4805
Actually we sold it but just like to lurk

Re: Results of ten coach bucks spent

Reply #15
Your fuel savings will pay for that new top-end in no time.

Hope you enjoy it.

Re: Results of ten coach bucks spent

Reply #16
only perfect machine has no moving parts.

SOB's ISL's have had fuel pump issues,  similar coach bucks. 
"Riding and rejoicing"
Bob
1997 U320 40' Mid entry, build 5132,  wtbi ce27, 4th owner
2007 Solara convertible
2 prodeco tech outlaw ss electric bikes

1095 watts solar
08 Ls 460 and a sc430
2000 Ford F-250 superduty 4x4

Re: Results of ten coach bucks spent

Reply #17
Hans, yes the new head has the same old "ears" as the original one. So much for experience-driven engineering.
Larry
1996 U295 36'
Build # 4805
Actually we sold it but just like to lurk

Re: Results of ten coach bucks spent

Reply #18
Hans, yes the new head has the same old "ears" as the original one. So much for experience-driven engineering.
Well, looks like another 160K miles before it may have another failure...... So, if 8k miles  per year that should put you at 20 years plus ... :o  ;)
Hans & Marjet
1995 U300 "Ben" (#4719)
3176B Cat,4060HD,Jake
SKP#139131
Motorcade#17579
2006 Honda Element (towed)

Re: Results of ten coach bucks spent

Reply #19
When I had the head gasket replaced in our U270 they broke 5 bolts, the old timer in the shop put the on his bench, ground the bolts flat with the head, center punched the bolts, drilled them to a thin shell and used a cape chisel to remove the bolt threads, I took the manifold to the race shop and had Joe surface it and elongate the holes, went together with no leaks, this was at a Cummins shop,there arn't  many old timers left to work on the old mechanical Cummins, total bill $1785.00
The selected media item is not currently available.Bill&Doris 97 U270 36'
University of Parris Island Class of 66
Semper Fi  Build# 5174 MC#17094

Re: Results of ten coach bucks spent

Reply #20
This is the method I have used in repairing heavy equipment. My brother broke one of his exhaust studs on his C7 cat when changing the exhaust gasket. I used my portable welder and removed it while still on the engine. People that don't know this trick are amazed.

http://www.youtube.com/watch?v=uwbb9Oj7VAg
1999 40 ft. U-320 wtfe build 5563 Chuck & Lynda's "Rollin' Inn"  2030 watts solar
prev. mh's 71 GMC 5 yrs. 73 Pace Setter 1 yr. 78 Vogue 5 yrs 81 FTX 40ft all electric 18 yrs. 1996 Monaco Signature 3 yrs.
2014 Grand Cherokee Overland
Dream as if you will live forever. Live as if you will die today.  James Dean

Re: Results of ten coach bucks spent

Reply #21
This is the method I have used in repairing heavy equipment. My brother broke one of his exhaust studs on his C7 cat when changing the exhaust gasket. I used my portable welder and removed it while still on the engine. People that don't know this trick are amazed.

http://www.youtube.com/watch?v=uwbb9Oj7VAg
Changed out many a head bolt on 335's using a buzz box Lincoln
'02 40' U320t  4010WTFS Build 6036 1 slide
Motorcade # 17841
SKP 151920
Retired truck driver
 5 million miler
Still have itchy feet for travel

Re: Results of ten coach bucks spent

Reply #22
tig heat, quench, often works too
1998 U270 34'

Re: Results of ten coach bucks spent

Reply #23
Wasn't a problem that there was no way to get the broken bolts out, the problem was a time factor and cost per hour factor. Didn't want to send the welder's kids through all four years of college so opted to send the dealer's kid through one semester.
Larry
1996 U295 36'
Build # 4805
Actually we sold it but just like to lurk

Re: Results of ten coach bucks spent

Reply #24
This guy is good, if I would of had a swig of beer in my mouth it would have exited my nose! Now I just have to stop the music from playing in the background of my mind. Please take me home.

Rock on

This guy is good, if I would of had a swig of beer in my mouth it would have exited my nose! Now I just have to stop the music from playing in the background of my mind. Please take me home.

Rock on

Here we come to Nac and spend moan-ay, moan-ay...hey guess what...get fixed...
Mike and Mari
'98  36 270 WTFE
Build #5272
Club #17504